It's been awhile! Seems like there hasn't been any time to post lately, and there still isn't, so I'm just checking in with a few shots of a Conn 26M VIII alto sax that I had the privilege of overhauling last month. If you want to read a well-written and informative article about the 26M, there's one here on Matt Stohrer's blog. Matt's posts are always thoughtful and insightful. Anyway, here's mine:
This instrument was in beautiful condition, and was brought in by the son of the original owner. His father passed it along to him when he was in second grade and it was the first saxophone he played. SECOND GRADE! He must have been the most coordinated eight-year-old who's ever lived, because this thing had no dents, no significant misalignment, and no missing parts. All of the (numerous) adjustment plates were intact and only a couple were frozen, and those broke free with a reasonable amount of effort. The only notable damage was that several of the pearl rollers were cracked and broke apart from being rusted on their rods.
The overhaul was a big job, but once all the pre-padding work was done (cleaning, straightening the body, aligning posts, fitting keys, leveling and dressing tone holes), the padding process was enjoyable, and the setup after that was downright idyllic. Need to adjust a regulation? There's a screw for that. Want to to change the key heights of the entire lower stack? There are screws for that. Want to change the relationship of the touchpieces in the left hand pinky table? That's more complicated than just turning a screw, but a hell of a lot easier than any other sax. This instrument had a steep learning curve, and I don't know how long it will be until I get to apply what I learned to another 26M, but it sure was a lot of fun.
Thursday, October 20, 2016
Monday, February 1, 2016
Sleeving the Upper Joint of a Clarinet Part 2: Graphite Banding
With
the sleeve in place and the bore restored to a consisent and
concentric shape (see previous post) I moved to the outside of the
instrument. The two enormous cracks running down either side of the
upper joint could still leak or even continue to grow, especially
with a plastic liner that expands at a different rate than wood with
temperature and humidity changes. While I usually choose to pin
cracks because of the relative ease of installation and minimal
cosmetic damage, that wasn't a feasible option in this case.
Drilling holes for the pins would have required going through wood,
then plastic, then wood again, and since different speeds are
necessary for drilling plastic and wood there was a good chance of
either overheating/burning the wood or melting the plastic. So
installing bands, while more cosmetically disruptive, made a lot more
sense. If you saw the previous post about this instrument, you saw that it came in with metal bands installed, which is an older method of doing this repair. However since the development and proliferation of graphite ribbon, sometimes also referred to as carbon-fiber, that's become the preffered material for banding. It's easier to work with and slightly more flexible than nickel, so there's less chance of it causing the bore to constrict as the wood expands and contracts over time (as had happened with this instrument).
Ideally I would have cut the channels for the bands deeper than in this example, so
that they could be installed below the surface and covered with
mixture of super glue and grenadilla dust, a technique I first heard
about from a technician in the UK named Chris Peryagh. But since a
lot of wood had already been removed from the inside of this
instrument, I tried to minimize the depth of the channels and
therefore keep as much wood as possible between the band and the
sleeve.
Before
cutting the bands, though, the top three tone holes had to be
re-drilled since they were covered up by the sleeve. Cutting a new
tone hole would ideally be done on a mill to ensure an absolutely straight
and level cut with an even pad seat. In this case since the top half of each
tone hole was still intact I was able to use that as a guide for
drilling out the sleeve on a drill press.
Re-drilling the C trill tone hole. Do you like my expertly constructed clamping jig? |
Wax is applied to the outside of the joint to prevent epoxy from sticking to the surface. That's the goop you can see in the top couple tone holes.
|
Next the channels were cut on the lathe to .040” deep. Epoxy will adhere in the channels since the waxed area was cut out.
|
The rest of the excess is filed off, then sanded until the bands are flush with the body of the instrument and the surface is smooth. |
The joint was immersed in oil for a week, then allowed to dry for about 3 more weeks so it had a chance to fully absorb as much oil as it needed. This is how it looked at the end of that process. |
After installing all new pads and corks and making a lot of fine adjustments, this instrument has a new lease on life. |
One last before-and-after, how the instrument looked when it came in, and just before packing it up in the case.
|
Labels:
Neat instruments,
Projects
Location:
Kenilworth, PA 19465, USA
Tuesday, January 19, 2016
Buffet English Horn Bonus Post 3 - Bore Repair
Prologue:
I didn't do this repair. In this scenario, for once, I was the
customer. David Teitelbaum did this work, and reminded me of my vast
appreciation for the skills of more experienced and seasoned
technicians like him. His skills and the quality of his work made the
full restoration of this instrument possible. Beyond that the insight
he provided into his process was immensely informative as I worked on
the clarinet bore sleeve detailed in this recent post. More on that
later...
Rebuilding
my personal english horn was a labor of love. But it was also a labor
of wanting to have a functional english horn. So after putting in
that time making parts and sealing cracks and fitting keys and
replacing pads and corks I ended up with an instrument that was
playable. Technically playable. But it was only after putting in all
that work that I looked for other underlying problems. My approach is
not always methodical.
I'd
observed that something was weird with the bore upper joint, but I
see lots of weird stuff and didn't worry about it. Turns out I should
have. The more I played the instrument, the more it seemed to
misbehave. Low notes would growl as if trying to jump the octave.
High notes were difficult to bring up to pitch. Intonation throughout
the instrument was very inconsistent. In searching for the cause I
found a crack
in the upper joint that
was causing problems. After that was pinned and sealed the whole
range became a little easier to play. Then I made a new
octave mechanism on
the suspicion that the original, convoluted mechanism was causing the
octave pads to not seal. That made the low notes more predictable,
but not great. Something
still wasn't right.
Something was still horribly wrong. I continued to recheck the pad
work and regulations, making adjustments wherever possible. It was a
shot to my ego to not be able to play an instrument I'd put so much
careful work and dedicated so much time to.
All
along that weird spot in the upper joint was in the front of my mind.
I knew it was probably the cause of all those problems, but was
reluctant to face that fact after putting in so much time on the rest
of the instrument. What if it couldn't be fixed and all of that work
was for nothing? How could I have been foolish enough to put in all
that work while overlooking something so serious? But like a
papercut, you can't look away and wince forever. Eventually you have
to open your eyes and inspect the damage. Then you get someone in New
York to make you a new thumb and graft it on. Nevermind, the analogy
kind of breaks down there.
Really
taking a close look and seeing how horribly the bore had been gouged
out I felt at once exasperation and relief. Exasperation at having my
fears confirmed, that I had put so much time into an instrument with
such a glaring and fatal problem; relief that maybe my work didn't
suck so much after all. It looked like someone had gotten a swab
stuck up there and had just gone to town with a screwdriver trying to
get it out. (When David called me with his assessment, he said it
looked like someone had drilled it out.) It was a surprising amount
of damage. The fact that the instrument played at all was remarkable.
I
was in a tough spot because I strongly suspected that this repair was
beyond my abilities. (Hindsight: Yeah, it totally was.) But I had put
a lot of time and effort into this instrument, and wasn't prepared to
let it be a total failure yet. Fortunately a conversation with
another oboe technician yielded the good news I needed: it could be
fixed, but there were only two techs in the US who would attempt it.
He advised calling David Teitelbaum.
So
I called and shipped it off. David called me when it first arrived at
his shop to talk about how intensive the work would be and the
likelihood of success (he was cautiously optimistic, but I had the
utmost confidence), and then I just sort of waited for another call.
This was the first time I've been an instrument repair customer in at
least a decade and it was unusual. Usually I know exactly what's
going on with a repair, but this time, with my own instrument, I just
knew that it was in the shop and would be done at some point and
would play better than it had. I hate not knowing, but the experience
was a reminder that I need to do a better job communicating with my
customers about the progress of their repairs.
Skip
to five weeks later and I got another call that the repair had been a
success and everything was good to go. A few days later I was playing
it and it was thrilling. David took the instrument and brought it
back from the brink of uselessness. Where before I could sort of
muscle my way through some passages, now it just plays. It plays
easily! And consistently in tune! It's a powerful instrument. There's
not a great deal of depth to the sound, but it will really project
through an ensemble texture. And whatever it lacks in nuance it makes
up for in ease of playability.
What could have quickly become a folly on my part was redeemed by someone who took the time to develop their skills. I always hope that people will be excited to play their instruments after I've worked on them, so it was nice to be on the other side of that transaction.
I
am regularly impressed by the skills of other technicians made
evident through their work, and I'm fortunate to see work that is
inspiring and informative from colleagues who are willing to share
their experience. In this case, hearing David's explanation and
asking a few good questions was helpful in developing a strategy for
the clarinet bore graft that I just completed. Between the insight I
got from talking to him and Mark Jacobi, that instrument went from a
lost cause (in my hands), to a long shot, to a feasible job, to a
successful and completed repair. It was exciting that while David was
doing that work on my instrument, I was able to do a similar (but
lets face it, much simpler) repair for my customer.
It's
invigorating to develop and refine a new skill that can be useful to
another musician. It's exciting, too, to be that musician and know
that someone who has spent years honing their skills is putting them
into practice on your instrument. I was grateful at having this
opportunity to be reminded of those things.
Labels:
English horn
Location:
Pottstown, PA, USA
Tuesday, January 5, 2016
Low A Oboe
I had this fun little guy in a few weeks ago. The owner said that, among other issues, the Low A mechanism wasn't properly regulated. How he realized that, I don't know, but it certainly wasn't from all the demanding Low A passages out there. Maybe he plays a lot of full range scales.
It was fun to work on, and the owner couldn't have been more pleasant. The Low A mechanism is pretty straightforward; it's activated by a right thumb touchpiece and is designed to also close the Low B and Bb keys, so you can go straight from C to A just by depressing the thumb. The only complication is that there are two regulation screws between the Low B and Low Bb keys. One is to adjust the regulation when playing low Bb, the other (visible in the center of the following photo) is to ensure that the Low B closes when playing Low A, which is tricky because of the flexibility of the very long mechanisms. It took a couple minutes to figure out, but now I'll be ready when the next one comes across my bench in 2038.
I hate that bench. Damn, we need a better consultation space.
Labels:
Neat instruments
Location:
West Chester, PA, USA
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